Drilling & Production Technology ›› 2019, Vol. 42 ›› Issue (4): 84-86.DOI: 10.3969/J. ISSN.1006-768X.2019.04.24

• DRILLING & PRODUCTION EQUIPMENT • Previous Articles     Next Articles

 Development of a new fishing tool for downhole throttle and tests

  

  1.  CCDC Downhole Service Company, Chengdu, Sichuan 610051 , China
  • Online:2019-07-25 Published:2019-07-25
  • Supported by:
     

井下节流器用新型打捞筒的研制与试验

马胜吉   

  1.  中国石油集团川庆钻探工程公司井下作业公司
  • 作者简介:马胜吉( 1986 - ) , 工程师, 主要从事特种设备维修及金属结构制作技术管理工作。 地址: ( 610051 ) 四川省成都市双流区协和街道华府大道二段 1405 号井下作业公司华阳生产基地机械厂, 电话:028 - 85764129, 15208483344, E-mail: mashengji542@ 126. com
  • 基金资助:
     

Abstract:  In order to achieve economic recovery and increase gas production rate, special tools should be used to remove the throttle or replace the throttle. The existing fishing tool for downhole throttle is not easy to control by coiled tubing, no flush circulation passage and with low fishing success ratio. A new fishing tool has been designed with a release fishing barrel, connected with six brass pins. The tensile and shear tests of the pin and fishing tool show that the design scheme is feasible, able to meet the needs of coiled tubing operation on site, and the success rate of fishing is improved.

 

Key words:  , downhole throttle, fishing tool, structure design, test 

摘要:  为了实现经济开采,增大采气量,需要采用专用工具取消节流器或更换节流嘴。基于对某油田中井 下节流器用打捞工具存在打捞成功率低、连续油管操作不易控制、无冲洗循环通道的问题分析,文章设计了一种新 型打捞工具,采用可退式打捞筒方案,6颗黄铜销钉进行连接,通过设计计算及打捞筒拉伸试验表明,该打捞工具设 计方案可行,可较好地满足该油田连续油管的施工作业,提高打捞作业的成功率。

关键词:  井下节流器, 打捞筒, 结构设计, 试验研究

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